U.S. Confidential - British Secret
Headquarters Allied Air Forces
Directorate of Intelligence
APO 925
Technical Intelligence Report
No. 163

Subject: Recovery and Reconstruction of
Type 0 Mk 2 SSF HAP
Air Technical Intelligence Unit
16 September, 1943
U.S. Confidential - British Secret

Reconstruction of Japanese Type 0 Mk 2 SSF HAP

SUMMARY

                This report is an attempt to give the complete story from the time of capture to the actual flight tests of the Type 0 Mk. 2 SSF HAP which was reconstructed by the Air Technical Intelligence Unit of Allied Air Forces.

                As far as possible, all discussions are in chronological order.

                A complete set of photographs from the time of capture accompany this report and show in detail many operations which are difficult to describe by narration.

CAPTURE AND SHIPMENT

                The airplane to which this report refers was captured on Buna Air Strip Papua, New Guinea, on December 27, 1942.

                As soon as the strip became tenable, Technical Intelligence Inspectors made a complete inspection, and removed instruments and small fittings, which necessarily had to be protected from souvenir hunters.  Immediately after, a detachment of seven enlisted men from a U.S. Service Squadron, under the direction of the Technical Inspectors, began the work of dismantling the airplane preparatory to shipment.

                Preliminary examination showed that a least two airplanes, all the engines available and other small parts would have to be salvaged to assemble one complete airplane.  The party worked about twelve days inspecting the airplane dismantling, preparing for shipment and removing it to Buna Beach, approximately 1000 yards through coconut groves.  Salvage work required considerable ingenuity on the part of the personnel concerned as very few tools and heavy equipment were available.  An engine hoist and jeep trailer together with a Japanese truck which was capture on the strip were sufficient to complete the job.  When extra personnel were needed for lifting and loading, much valuable assistance was rendered by the Australian Troops stationed at Buna at the time.  A barge was secured and an attempt was made to load the salvage at Buna Beach.  After three engines had been loaded, a storm came up and the barge sank before morning, dropping two of the engines into the sea, and damaging the hoist beyond repair.  The following day, the submerged engines were salvaged and treated as well as could be with available engine oil.  A larger steel barge was then supplied and the loading was continued without mishap.  The larger barge proved to be adequate to transport all of the salvage on one trip, and it was towed to Ono Bay, eight miles distant, on 1 February, 1943.

                The following day the equipment was transferred to a small freighter and sent on to Milne Bay that afternoon.  One officer and four enlisted men accompanied the shipment as some little trouble was experienced with soveniring.  A policy of strict, *HANDS OFF* was then established, and no parts were stolen.

                After arriving at Milne Bay on the first of February, further transshipment was necessary to a larger freighter, which was bound for the Australian mainland.  This freighter left Milne Bay on February 9, and arrived in Brisbane, Australia, on the 19th of February.  On this part of the journey, the equipment was locked in the hold and a guard kept on the hatch at all times.  This was necessary due to the persistent efforts on the part of personnel to inspect and souvenir the equipment.  Upon arrival at Brisbane, the equipment was immediately taken to the A.T.I.U Hanger on Eagle Farm.

                After complete examination and recommendations, the Command, Allied Air Forces, decided to reconstruct one airplane and run test flights here rather than ship immediately to Wright Field.  This decision bore the condition that the reconstruction of this airplane would not interfere with the repair and assembly of operation airplanes.  The reconstruction of this foreign type airplane necessitated the assembling of sufficient tools, materials and supplies, plus trained personnel to do the highly technical work involved. 

                After a careful re-examination of all component parts of the airplane, it was found that more damage than that which was first apparent had rendered the airplane difficult to repair.  This damage was caused chiefly by intensive aerial strafing, bombing, small arms and medium caliber ground gun fire, together with damage purposely inflicted by Japanese personnel and souvenir hunters, both Japanese and American.  IN addition, minor damage was incurred by two of the engines as a result of having been submerged in salt water.

The following is a list of parts shipped:

a)  Four engines.

b)  Five propeller assemblies.

c)  Two main fuselage and wing sections, including ailerons and flap

d)  Two rear fuselage sections.

e)  Two tail assemblies. 

f)  Two landing gears and two tail wheel assemblies, three tires.

g)  One extra oil tank and one extra fuel tank.

h)  Two sets engine cowling.

i)  Two batteries

j)  All instruments and small control equipment available. (At least two of most items).

k)  Available armament, which included 20 mm. Cannon and 7.7mm. machine guns.

l)  Miscellaneous small items, such as fairing, wing tips and engine accessories.

DETAILED SUMMARY OF REPAIRS OF COMPONENT PARTS

1. Engines

    Four engines were removed from the airplane on the field and as before stated, two of these engines received slight damage due to submerging in salt water.  From parts available that appeared to be fit for operational use, it was decided that only one engine would be rebuilt.  This was based on the fact that nose sections, power sections and numerous cylinders had been pierced by bullets.  Carburetors, accessories and oil coolers had been extensively damaged but one or more of all components parts were definitely available.

    As repair facilities in the Brisbane area were not available, all engine material and two mechanics were sent to U.S. Air Corps Civilian contract shops in Melbourne.  The main factor encountered during overhaul was corrosion which made it necessary to spend a great deal of time in cleaning parts for reassembly.  The advanced state of corrosion is explained by the fact that these engines had been immobilized for at least six months, five of which had been spent on the Buna Strip and in shipment from there to the repair facilities.  The engines selected for final repair came from the same main fuselage section as the airplane selected for repair.  The engine selected for final repair came from the same main fuselage section as the airplane selected for repair.

    Magnetos as well as the oil cooler were taken from another airplane.  Most of the time consuming element other than the cleaning of parts was the making of piston rings, gaskets and seals.  Cylinders were ground out to depths ranging from .002 to .007 depending on the depth of corrosion.  Attempts to manufacture the top chrome plating ring were unsuccessful and the original top rings were used and locally manufactured rings were used for the remainder.

  Upon completion of repairs the engine was given thorough block test and about twenty-three hours on a dynamometer test stand.  Results of the dynamometer test were published in Air Technical Intelligence Report No. 159.  At the conclusion of these tests, the engine was dispatched by air transport and arrived in time to be installed in the completed fuselage.

2.  Propeller.  Five completed propeller assemblies were secured on the field and shipped.  It was planned to assemble two complete serviceable propellers from component parts available.  Nearly all of the blades and some other components were bent, holed by bullets, or corroded.  All parts which appeared to be repairable were then shipped to the Airscrew Division of DeHavilland Aircraft, Pty. Ltd., Sydney, for major overhaul.

                Propeller No. 79776 was repaired to specification with the exception of No. 2 blade, Serial No. 55040, which is slightly thin on the trailing edge tip station and has waves on the camber side, caused through numerous indentations from the 42" station to tip.  This propeller is qualified for full flight test.  Upon completion of repair this propeller was immediately shipped to Eagle Farm, Brisbane, to await flight testing of the airplane.  It arrived in good condition.

                Propeller No. 80560 was repaired for use as a secondary propeller as not enough repairable parts were available to assemble a complete first class unit.  All parts were repaired to specification except blade Serial No. 55079 which has pronounced indentations on the face on the 22”, 25=3/4” and 50” stations, and blade Serial No. 55080 which has pronounced indentations on the 49" and 53" stations.  These blades were released for limited flying only.  Upon completion of repair this propeller was sent to Melbourne to be used in conjunction with the testing of the HAP engine.  It was later shipped to Eagle Farm and arrived there in good condition on Jun 17, 1943.

                Two constant speed governors have been repaired and tested and are ready for use.

3. Main Fuselage and Wing Sections.  Many sheet metal problems were encountered in the repair of the main fuselage and wing section of the plane because of the extensive damage caused by the aforementioned intensive aerial-strafing, bombing and ground fire.  This damage, coupled with the fact that the HAP type airplane is definitely not an easily repairable type resulted in the consumption of excessive man hours of skilled labor.  Chief among the difficulties were the bullet holes which ordinarily passed completely through the structure making numerous holds for every individual bullet.  A complete detailed description of these repairs cannot be given but examples are described and shown in some of the photographs.

                Of the two main fuselage and wing sections the one which appeared to be the most structurally complete was chosen for repair.  This was airplane No. 3030.  No. 3032 possibly had less bullet holes but its repair was precluded by the fact that approximately six foot of the right wing was torn off apparently as a result of a bad landing.  Some parts were used from No. 3032 to replace damaged ones on No. 3030, but in general new ones had to be fashioned to insure a proper fit.

A.     Fuselage - Left Side.

The left side of the fuselage was damaged comparatively little, and required only a few flush patches to complete the repair.

B.     Fuselage - Right Side.

Right side of the fuselage required about ten flush patches on the front half and complete new skin on the rear half.

C.     Fuselage - Internal.

Repairs to the interior of the fuselage were extensive.  They included the replacement and repair of a number of stringers, formers and backers.  Most of the control cables, electrical wiring and lines were destroyed or damaged severely in this section necessitating replacement.

D.     Wing - Left.

Both wings were damaged severely and required extensive and painstaking repair.  As noted above the accessibility of nearly all parts of the wing was very poor.  The left wing was holed through in many places by bullets and shrapnel and many parts of the ribs, stringers and spars required replacement or repair.  Repairs to the small parts were accomplished by installing new ones.  Skin repair was kept flush either by using flush patching  or installing new skin of comparable thickness to the original.  The greatest single difficulty came in the strengthening of extruded T sections which comprise the flange members of the spars, and which were shot through by projectiles.  Dural angels were machined carefully to fit the T section and were either bolted or riveted in place, depending upon the pace available and the amount of shear the splice was required to withstand.  Now pitot lines and electrical connections were installed as the repair was completed.

E.     Wing - Right.

The right wing presented the same difficulties as the left, but in a much more intensified form.  Damage was very extensive near the wing root and flap section as a result of the explosion of a "daisy cutter" bomb nearby.  The entire section from the rear spar to the trailing edge for a distance approximating the flap length was rebuilt completely.  The spar was repaired by the use of the specially machined dural angles as in the left wing.  As the old structure of the wing would not fit after allowing space for the spar repairs, the adjoining parts were of necessity, redesigned.  Spar splices were checked for adequacy of reinforcement necessary and aircraft bolts used when any doubt of the available space for rivets was evident.  Some flush patching was used on this wing but much of it was recovered with new skin.

F.     Flaps.

As noted above the flap in the right wing was nearly destroyed by the explosion of the anti-personnel bomb near by.  This required its complete repair or replacement together with the lines and actuating mechanism.  Sufficient parts were procured from Aircraft No. 3032 to make a complete operating unit.  The left flap presented less trouble and was completed in good time.  The interconnecting cable for the flaps on both ships  tested was rigged to an extremely high tension and was definitely over three hundred pounds.  This was thought to be in error and appeared much too high as the supporting brackets were failing on both ships.  The cable on final repair was rigged to approximately two hundred pounds of tension.  Flaps worked well with this set-up.

G.     Wing Tips.

The wing tips were fitted from available ones and then repaired.  Some work was required on the plexi-glass wing tip lamp covers which were reformed from new material.

H.     Canopy.

Neither the canopy from No. 3030 or No. 3032 were repairable, but one from a previously captures Zeke was fitted. 

4. Rear Fuselage Section.

A.     Fuselage.

It was decided to use the rear fuselage section from Airplane No. 3032 as it appeared to present the least problems for satisfactory repair.  It was damaged very severely as the result of shell-fire and souvenir hunting.  No. 3030 was rejected because it had been blasted out of shape by bomb concussion.  Numerous small parts were secured from it, however, to assist the restoration of No. 3032.

As most of the skin covering was so badly holed nearly the entire section was recovered with skin of comparable thickness to the original.  Stringers, formers, brackets and other small parts were either replaced by parts from the other fuselage or they were fashioned new.  Nearly all control cables and electrical wiring were replaced as the original was all practically destroyed.

B.     Fin.

The vertical fin was damaged to the extent that it involved removal of the skin covering to repair the internal members.  These were all strengthened to at least initial strength.  Fairing was fitted from the best available.

C.     Horizontal Stabilizers.

These presented no unique problems for repair but some time was consumed, as the flush patching necessary was difficult to rivet in the small spaces.  Bother were fitted up well to the fuselage.

5. Flight Control System.

A.     Ailerons.

Numerous dents, bends and bullet holes rendered the ailerons inoperative without considerable repair.  Trailing edges had to be entirely replaced as well as a number of the ribs.  Covering and doping was done according to U.S. Specifications.

B.     Elevators and Rudder.

These occasioned less repair than the aileron after the best units of the lot had been selected.  Nevertheless, considerable time was necessary to put them in first class condition.  Covering and doping was done to U.S. Specification.

6. Landing Gear.

A.     Main Gear.

Both main landing gear legs were completely removed, inspected and repaired where necessary.  The left leg of No. 3030 was shot through with a heavy caliber bullet necessitating its replacement from other parts available.  Parts were not interchangeable to a high degree, so much hand fitting was required.  Several tests of the fluid contained in the oleo leg and retraction mechanism and of the hydraulic system fittings showed the fluid contained in the oleo leg and retraction mechanism and of the hydraulic system fittings shoed the fluid be a mineral base type.  It was therefore decided to use U.S. Air Corps Specification 35800 Grade M Medium fluid in place of the original.

B.     Tail wheel.

The tail wheel was completely disassembled, inspected and repaired where needed.  No particular trouble was experienced in obtaining a complete operating unit.

C.     Arrestor Hook.

Arrestor hook was not damaged, so needed very little attention.

D.     Tires.

Three main wheel tires and tubes were selected from those available and sent to and airplane tire manufacturing firm for complete reconditioning.  Upon receipt of the tires from the repair shop they didn’t appear to be entirely first class condition so investigation was begun to find one of our own tires that would fit.  This turned out to be the general 22 x 6.50 x 10 4-ply, and appeared to be entirely satisfactory.

7. Tanks.

A.     Fuel Tanks

Both wing tanks and the fuselage tank required considerable repair as they had been holed in numerous places.  As the tanks were not of the self-sealing variety and repairs were accomplished by welding.  All tanks were then subjected to fluid and pressure tests as specified in technical orders for U.S. airplanes.  Test pressure was limited to that specified by the Japanese.  Now chafing strips were installed.

B.     Oil.

The fuselage oil tank was repaired in the same manner as the fuel tanks and tested for leakage.  Now chafing strips were installed and tank was re-varnished.

C. Hydraulic.

       A new plug was the major repair on the hydraulic reservoir tank.  This was machined and metric threads cut on it.

8. Cowling and Fairing.

                In general cowling and fairing was not difficult to replace as there were a number of spares available.

A. Engine cowling was fitted and needed very little repair except the oil cooler scoop which was completely rebuilt.  Shutters were in good condition.

B. Propeller spindles were in general, badly damaged, but one was available which appeared to be serviceable with a small number of patches.  This was repaired and was suitable

C. Formation and navigation light covers including those on the wing tips and tail cone were either badly damaged or missing completely.  These were remolded from plexi-glass by a commercial firm.

9. Instruments.

                Two complete sets of instruments and some spares were shipped from the field, and from these, two sets were repaired and calibrated.  The main difficulties encountered were corrosion, the effects of shell fire on delicate parts, and the method in which the instruments had been removed from the ship.  Much time was spent in cleaning and fitting of small parts, and refinishing.  Tracing and replacing various connections presented some difficulty as no information of their original position was available.  Japanese instruments were used throughout excepting the free air temperature gauge.

10. Gun Sight.

                Three reflector gun sights damaged to varying degrees were on hand and from these, one was placed in serviceable condition.  Repair consisted mostly of cleaning, repairing and replacing damaged parts.  Two glass reflector plates were manufactured locally.  The lens assemblies were in particularly bad condition, and it was necessary to use lenses from all three units in order to get a serviceable set.  As the original light was missing, an American bulb was substituted, necessitating some adjustment in the lens assembly to obtain the proper image.

11. Electrical

                Two main junction box and switch panel had been left intact in airplane No. 3030, and only a few repairs were necessary on this part of the system.  However, the lines in both wings and the tail had all been damaged by gunfire and for the most part were completely replaced.  All cockpit lights and fixtures had been removed and were replaced with like kind in so far as possible.  American bulbs were substituted throughout the airplane.

12. Pneumatic System.

                This system was particularly difficult to replace because of the fact that all component parts and connecting line had been removed, and no previous information on the system was at hand.  Parts of this system had previously been connected with the oxygen system, adding some difficulty in their straightening out.  After completing the oxygen system,  and eliminating the pneumatic system parts which had been connected to it, the system took definite shape and was completed after expending much work in the repair of the units and replacement of connecting lines.  No air compressors were sent from the field with the shipment of HAPS.

13. Oxygen Equipment
                An attempt was made to install the original Japanese Oxygen system complete, but while the parts were in storage, the only good oxygen regulator on hand was taken from ATIU and never returned.  Consequently, an American type regulator was installed in the airplane and adaptation made to the original system.

                A high pressure system was retained because the Japanese oxygen bottles were fitted in particular place and no American bottles were found that would fit.

14. CO2
                This system was complete, and the only work necessary was refilling the supply bottle.

15. Radio
                No radio equipment was captured with the airplane, excepting the radio compass installation, which was very similar to Fairchild installation.  This was replaced and installed in the airplane.  For added communication, a search was made for a small set which would not be heavy in weight and occupy very much space.  The U.S. SCR-183 radio set was selected and installed in the airplane.  Much trouble was encountered in perfecting satisfactory setup, but it was finally accomplished and was proved quite successful.

16. Brakes.
                As the project neared completion and the airplane was ready to fly, it was found that the brake system in the airplane was very poor.  This was probably due to the rather weak landing gear installed on the airplane.  An attempt was made to strengthen the brakes but this was finally abandoned when it became apparent that no repairs other than a major modification would give satisfactory braking.  It was decided that the brakes should never be used except in extreme emergency.

17. Finish.
                The outside appearance of the aircraft upon completion was very poor and a new finish was applied.  A study was made of the original finish as to weight color and texture, and comparable paint of a lacquer type was selected and applied.  A dove gray color was used for the fuselage, blue for engine cowling and red for trimmings.  The U.S. AAF "Star" was painted on the airplane except for photographic purposes when the original Japanese markings were applied. 

18. Armament
                Sufficient armament was recovered to insure a complete set of 2x20mm cannon and 2 x 7.7 mm. Mgs. For the HAP.

Flight Tests
                The initial flight test of HAP was performed on 20 July, 1943, at Eagle Farm.  This flight was for 25 minutes duration to test the trim of the airplane.  No trouble was encountered and no adjustments were necessary except trimming.  Succeeding flights were made on 21 July, the second of which resulted in some damage to the airplane from ground looping after a dead stick landing.  The engine cut out on a slow roll and never recovered due to carburetor trouble.  The right landing gear was damaged sufficiently to require replacement.

                It is believed that a grabbing brake probably caused the ground loop as no tendency was noted for ground looping on the first two flights.  After the right landing gear was repaired, the airplane still had a tendency to ground loop the opposite way so a tail wheel lock was secured and installed.  Since that time, no further mishaps of this nature have occurred.  At no time have brakes been good even after much time and effort had been expanded in relining, adjustment and checking of the system.  Consequently, all pilots have been ordered not to use brakes except in extreme emergency.

                Since beginning flight, some U.S. instruments have been installed including an altimeter, rate of climb, airspeed indicator, and free air temperature gauge.  In general, mechanical operation of the airplane has been good except for minor items.

                Numerous flights have been accomplished to the present time including altitude tests, speed runs, rates of climb, simulated combat against other fighter planes and for photographic purposes.  As noted above, full armament has been installed to duplicate original weights in order to give a true test of performance.

                Complete flight test results will be released as quickly as data becomes available.

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